Happy Easter everyone! I'm a church-goer, and Easter Sunday is the most important date in the calendar for me. But, this isn't the right forum and I will respectfully refrain from engaging with any further posts on that topic. I'll keep this update to the topic of boaty-stuff.
I remain convinced that there is a cheap fix in there somewhere, but finding the parts remains a mission. After the thread in the socket for the banjo bolt on my low pressure pump, I had to find out what it was. With a borrowed gauge and a thread-testing assembly, I found that it is an M10 with a 1mm pitch thread. I would like to fix it with a Helicoil insert, which is commonly referred to as a thread repair kit on retail websites. However, it is surprisingly difficult to find a 'real' shop that supplies them, and which is open at weekends. Repco, for example, was open on Saturday, but only stocked thread repair kits for M10 with a 1.5mm pitch. Next up, I'll try Blackwoods in Hamilton, but might have to resort to on-line shopping with the mandatory several-day wait and the uncertainty that I'll get all the bits and pieces that I need, like the right drill bit, tap and tap-spanner. I'll also try the Dowty washer option mentioned previously.
I also re-fitted the cut-out to my engine access hatch, and installed a squeezy bulb on the fuel line to help push out the air when I reconnect the lines. I have a couple of sets of better-quality hose-clamps and a stop-cock coming in the post, which should help to stop a couple of minor drips in the fuel lines. I ran the engine, just to check it. It ran OK, but sounded like there was some air remaining in the fuel lines.
It took a bit of boat-yoga, but I successfully removed the cover to the low pressure pump. The photo below shows it before removal (before you ask, I had begun to unscrew the lower near-side bolt before taking the photo). As I suspected, it is an alloy casting, which is relatively soft and vulnerable to thread-stripping. Now that I have it out, I can drill and re-tap it, confident that I will not leave a metal shaving in there to do some damage to the engine's innards. I'll borrow a mate's drill-press to get it properly aligned. The photo also shows some wetness around the high-pressure fuel line, which is becoming the prime suspect in the original leak.
If I fix the leak and avoid a large bill for a new motor, I might move on to the bearings, which have probably been hammered to death, the wiring, which is a frightening rat's nest of spaghetti, and the engine beds, which have some impressive splits in the glass along the edges. Even if I get a new motor, I'd have to do something about the wiring and beds in any case.